Boeing 737-377, G-CELA
During a climb to FL270 with autopilot ‘B’ engaged, the aircraft did not capture the selected altitude. The commander disconnected the autopilot and then experienced difficulty in accurately controlling the aircraft in pitch. He declared an emergency and was given radar vectors and an unrestricted descent to Stansted Airport, where he made a safe landing. The investigation revealed that a tripped circuit breaker for the autopilot stabiliser trim actuator had caused the failure of the aircraft to capture the selected altitude. No malfunction was found to explain the commander’s difficulty in accurately controlling the aircraft in pitch.
Boeing 737-377, G-CELA 04-07.pdf (770.47 kb)
Published 10 December 2014